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Stuart No 1
Conclusion

The comments and thoughts about the final model.

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1. The flywheel casting halves had some mis-alignment which meant it was impossible to get both sides running perfectly concentric

2. The sole plate was not symmetrical about it's long axis. This meant that the bearings had to be machined to compensate for the off-set of the top half of the engine.

3. The lower, rear corner of the connecting rod had to be chamfered to stop it hitting the bolt heads which held the slider plates in place. 

4. In combination with the con-rod modifications the heads of all the bolts had to be halved in height to avoid a clash with the con-rod.

5. The threads in the gland studs were not long enough and had to be extended to give a suitable clamping force on the gland packing, extra gland packing was also used.

6. I couldn't get a satisfactory fit with the valve guiding rod. This was missed off altogether.

7. The lower face of the steam chest had a crack on the inside. This could have been a casting fault or could have been caused my me over tightening the 4-jaw chuck.

8. The valve didn't operate when first tested. The steam chest had to be machined further, to get the valve block to mate with the port face on the cylinder. The valve block was also made a looser fit on the valve rod so that it could seat itself under steam pressure to give a good seal against the port face.

9. Initially the piston hit to top cylinder cover at TDC. This was corrected by shortening the piston rod and also by skimming the top of the piston.

10. The top face of the standard was still not square despite being machined twice. In the end filing and shim washers were used and the mounting holes at the top were opened out, to get everything to line up. 

Despite these shortcomings, the finished engine looked great and worked with a powerful stroke on compressed air.

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